Sep_03_1999_M44.txt Shift M44 Start at 1999:246:18:00:00 GMT = 1999 Sep 03 2:00pm EDT End 1999 Sep 03 10:00pm EDT SOT Lead Bill Podgorski SOT SC/ACA FOT-SI HRC-SI Steve Murray/Gerry Austin ACIS-SI Yousef Butt/Paul Plucinsky Plan: Run P10 HRC observations: - Complete 9000 sec observation of CAS-A as part of "standard candles" - Perform HETG software insertion/retraction testing via CAP 371 while in radiation zone EVENTS DONE OBSID -------------- ---- ----- Start Shift 246:1800 171 ----- Out of Contact------ Running HRC-I observation 171 ongo AOS DSS61 246:1800 ----- Real time------ End HRC-I 171 246:1805 Execute Rad zone entry ATS 246:1805 Start CAP 371 to test S/W insertion/retraction of HETG 246:1900 (see discussion below) End of shift 247:0200 NOTES/ISSUES/PROBLEMS --------------------- 1) CAP 371 was planned to test software insertion and retraction of the HETG. The initial insertion failed due to there being incorrect state flags in the OBC. These flags were incorrect due to the failed previous attempt to insert the HETG via software. These flags were corrected via real-time commands and the software insertion of the HETG via SCS 247 was successful. During the insertion, however, it was noticed that the telescope MCE-B (Mechanism Control Electronics-B) 28 volt motor drive voltage telemetry monitor was reading about 6.2 volts during grating motion, even though the motor was being driven by MCE-A. We expected the MCE-B drive voltage to be zero. Investigation of prior HETG flight insertions and retractions indicated that this voltage was present in every case (total of 5, 3 insertions and 2 retractions). It was decided to defer retraction of the HETG until the 0300-0400 COMM period while the problem was analyzed. A telecon was held at 6:00pm EDT to discuss the issue. Several possible causes of the problem have been identified. The most likely cause is that the voltage seen is due to back EMF generated on the B side (redundant) windings as the A-side windings are driving the motor. Both the A and B side windings are on a common shaft, hence there will be some voltage generated as the motor shaft rotates. The voltage level to be expected is unknown at this time. Kodak and TRW were tasked to look into this via both circuit analysis and test, using flight spares at TRW. A second possibility could be a short between the A and B side windings. This could be a more serious issue. A decision was made to retract the HETG during the day 247 0300-0400 (tonight) comm period, using the A side MCE. There will be another telecon to discuss the issue at 4:00pm EDT tomorrow (Saturday, Sept 4). The meet-me number will be posted on 617-496-7030. 2) Planned COMM: 246:1800 --> 246:2300 DSS61 247:0300 --> 247:0400 DSS16 (Retract HETG) 247:0845 --> 247:1030 DSS42 (Upload P11) 247:1815 --> 248:0220 DSS61 248:0215 --> 248:0415 DSS24 248:1030 --> 248:1215 DSS42 248:1600 --> 248:1800 DSS66 248:2200 --> 249:0330 DSS61 (Insert LETG) 3) Radiation Zone: 246:1830 --> 247:0523 4) Perigee: 247:0007 5) P11 Load: To be put out for general review at about 9:30pm.